Anonymous Railfan
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anonrailfan.bsky.social
Anonymous Railfan
@anonrailfan.bsky.social
Big fan of trains among many other things!
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Major HJR Enthusiast 🇯🇴🇸🇾
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Fan of the PRR, NYC, NKP & more!
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Late 20th - Early 21st Century steam historian(?)
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Btw Free 🇵🇸
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MASTODON: https://mastodon.social/@Anonymous_Railfan
My interest has been piqued, I shall investigate
December 4, 2025 at 2:46 AM
I've never understood New York's hostility to preservation. Like why, do they just have a vendetta or some crap? Whatever it is it's infuriating.
December 3, 2025 at 9:34 PM
From what I know that sounds about right, but advancements in traction motors made four axle and B+B arrangements redundant, which is likely why it wasn't repeated. I'd also imagine it was a bit of a mechanical headache too.
December 3, 2025 at 7:35 PM
Felt. Every time I try to cook it, it just doesn't.
December 3, 2025 at 3:02 PM
IT WAS NEVER AN M
November 19, 2025 at 5:55 PM
That's just based.
November 14, 2025 at 3:35 PM
*for almost a decade. Still can't grammar
November 13, 2025 at 9:50 PM
I can't even
November 11, 2025 at 3:39 PM
How gaudy
November 10, 2025 at 10:16 PM
And here is one of 600's sisters in her NdeM guise. Note the modification to the tender, as these engines were converted to burn oil on the NdeM. They were also reclassified as the UR-1.
November 7, 2025 at 11:51 PM
As an aside, there are a few sources running about saying that these were steam to diesel conversions, and I have NO idea where that came from or WHY the University of Pittsburgh's library system is parroting that. They have the full set of photos when all the changes were made to these engines. 🤷
November 7, 2025 at 1:59 AM
To be short, they were outright failures. The induced draft fans were rapidly eroded by cinders, and their soft exhausts essentially choked out their crews with smoke. Both engines were quickly retired and replaced by more modern 0-8-0s.
November 7, 2025 at 1:59 AM
Well, the combustion chambers and flues were shortened, induced draft fans were installed, and mechanical stokers and water level controls were added. Their tenders had their water and coal capacity levels increased, and mechanical lubricators were also added.
November 7, 2025 at 1:59 AM
transferred to switching and transfer service, it made sense to try and rectify this issue. This was also a cost cutting measure as well. So, two M2s were rebuilt between 47-48 and.. this was the result. Asides from the obvious cosmetic changes, what else was changed?
November 7, 2025 at 1:59 AM
I'd also like to know. I'm wondering if it has any full dimensions of the whistles used
November 5, 2025 at 10:24 PM